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January 29, 2014
05:15 EDTSSNSamson Oil & Gas provides operational advisory
On Tooheys 4-15-14HBK, flow-back operations on this well are underway and in the first 38 hours of this operation 1,589 BO and 3,778 BW were recovered, representing an oil rate of 1,000 BOPD. The well is being flowed on a 28/64th choke and is therefore not flowing at its maximum potential. It is currently anticipated that the oil rate will increase over the next week as the water production decreases and the well cleans up. While the flow back period measured is relatively short, it is nevertheless above the company’s pre-drill expectations. Flowback of Little Creature well was initiated but was curtailed because of a sand plug. A coil tubing unit has been rigged up to drill out the frac plugs. Flowback of Coopers well will follow the flow-back of Little Creature 3-15-14HBK well. Coopers, Tooheys and Little Creature are located on the Tofte 2 pad on the northern boundary of Section 14. The frac of the Blackdog is expected to commence February 5th. A coil tubing unit will be used subsequently to drill out the frac plugs in both the Blackdog and Sail and Anchor 1-13-14HBK wells, enabling both of these wells to be put into production. These wells are located on the Tofte 1 pad, which is on the southern boundary of Section 13 within the North Stockyard project.
News For SSN From The Last 14 Days
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July 29, 2014
05:08 EDTSSNSamson Oil & Gas provides operational advisory
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July 22, 2014
05:05 EDTSSNSamson Oil & Gas provides operational advisory
The 4-1/2 inch production liner has been set and cemented successfully in the Bootleg 7-14-15TFH well. Frontier Rig 24 is currently drilling the vertical portion of the wellbore at 8,549 feet on the Bootleg 6-14-15TFH. Once the Bootleg 6-14-15 TFH is drilled the rig will then be moved to the north pad and begin drilling the two Ironbank wells. A work over rig completed running the rod string on Matilda Bay 2, and the well is now flowing. The Matilda Bay 1 is currently undergoing a liner repair. Following this work over the fracture stimulation program will be completed. As previously advised further consideration is being given to testing a zone in the Bluff 1-11 wellbore in the primary target, the Permian Hartville Formation. The Gladys 1-20 H well is being drilled by Continental Resources. The well is a 1,280 acre lateral, approximately 10,000 feet, in the middle Bakken. The curve has been drilled and landed in the Middle Bakken, and 7 inch casing has been run and cemented and a depth of 10,436 feet. A work over rig was moved onto the well July 16th to re-establish production. Rods were parted at the top of the pump. Tubing was pulled to retrieve the pump. Tubing, rods, and a new pump were run back in hole, and the well was put on production July 18th. Since then, the well has flowed 317 bbls oil at a rate of 159 BOPD.
July 15, 2014
05:16 EDTSSNSamson Oil & Gas provides operational advisory
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